Yeah the gas is a good idea, Noel---LOL! Ran probably 4 minutes! I too pulled the choke and it ran a bit better, briefly.Great that you got it out. Gas does help them run. Happened to me last week end. Went to start the John Deere, so we could get the MF 16 in, and only would run if I kept the choke on. Thought, that’s kinda weird. Then all of a sudden, ahhhhh. Out of gas I bet. And sure enough that’s what is was. It had not run since January I think.
Any way. Don’t worry about the noise Doug. Run it for a bit. Change the oil again. See what happens.
Noel
Contact member "Ducky" to see if he still has some o-ring kits for the hydraulic control valves.Nice day today, and stayed nice until I got home from work! Opened the overhead door, fired up the K321, let it warm up a minute and got this far out of the shop before it died!
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Well no need to panic----it ran out of gas---LOL! Problem is that I haven't filled my gas cans yet. Probably scared of what 91 non-ethanol costs! I'll get them filled this weekend. Still think I was hearing a little "rattle" sound occasionally, but my bad hearing can't tell for sure, or where it's coming from.
Shoved it back in the shop and put the hood on it.
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Couldn't put Daniel's spool valve cover on yet, since the cap was on back order at one place and just recently got my money back. I will try Jack's now and start looking for the o-rings to rebuild the spool valve. I'm behind on some other stuff so it may not be right away.
DAC
HA! In my teens she was pretty darn sure she did, Chris! Nowadays, I ain't sure---LOL!Nice work Doug. Can tell your mother didn't raise no dumbbell.
I been lucky so far but I would hate for my luck to run out, Noel! Could be a bad day. Thanks.Nice fix Doug. Ya that would not be good getting any thing caught in the driveshaft.
Noel
It might disappoint you I'm not doing a restoration Jim, but that would be way more work than I want to do. I want this machine to work for me, not the other way around. Got several things to build for it yet to do my yard mule chores. So far it's a great hauler and gravel smoother with the grate I built for the 3 point.Wow 39 pages and I’m just now seeing this project, sorry Doug. That was a good fix. Believe it or not I just seen several of those tape deck brackets in some junk of mine. When I settle down tonight I’ll do some catching up.
That's a nice tail pipe DAC looks OEM bet it did make for a nice soundI had forgotten about this thread. Decided to put some work I did on the MF1450 today here. The driveshaft issues have been resolved so I have a lot more confidence in this thing being useable for longer than I had thought.
Today I drained the engine oil and decided to alter the muffler so it doesn't discharge right to the inside of the hood. Let the oil drain while I worked on a idea I got in my sleep a few nights back---LOL!
Some of you may remember that the heat exchanger in the shop furnace developed a hole in it last December. Fortunately it was still under warranty so they sent a new one free.
Threw the old one out in the scrap pile. Thought maybe the tubing from it may be useful sometime. Measured the OD of the muffler discharge then took the calipers out back and measured the ID of the heat exchanger tube. By some stroke of luck it measured about the same!
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Tested and it is very tight but still will go over the muffler discharge.
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Finished the oil change and cut the end of the muffler off. Cut a piece of that heat exchanger tube about halfway between two bends. Did a little beveling on the muffler and cut a couple of slits in it to give a little movement to drive the extension on. Drove it on with a no bounce hammer.
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It clears the hood nicely.
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Took the muffler off the engine and put it in a vise. Cleaned everything up with a wire wheel on a drill and got out the little torch. I didn't feel confident enough to use the mig to weld it. Decided to braze instead.
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Was a good way to have a race on TV while actually being productive---LOL!
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Let it cool, scuffed up everything and wiped it down with brake cleaner. Sprayed it with some high heat black and put it back on the tractor.
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Severe thunderstorm warning was posted so had to call it quits. Put away tools and ran that tractor outside. It didn't even sound like the same tractor! Much quieter! Now I can hear the noise of the Kohler internals---LOL!
Swept the floor and brought Loree's car in.
DAC
The exhaust passed through a hole in the front grill. This muffler isn't original. The OE had the exhaust pipe out of the front of muffler body.Yes it does look good Doug...imagine buying the one from the factory...!
Where did the original exhaust supposed to blow out ?
Not directly on the hood ?
Thanks Chris! I would be lost without my junk out back---LOL!That really turned out professional looking. Looks very good. What the heck would a guy do without an iron pile.
No way I could justify buying MF original parts for this beater Bill! I appreciate your comment! Daniel answered the question.Yes it does look good Doug...imagine buying the one from the factory...!
Where did the original exhaust supposed to blow out ?
Not directly on the hood ?
Thank You Gary, still pulling for you two to get home soon!That's a nice tail pipe DAC looks OEM bet it did make for a nice sound
This is what the muffler looked like when I brought this thing home over 4 years ago now.The exhaust passed through a hole in the front grill. This muffler isn't original. The OE had the exhaust pipe out of the front of muffler body.
Doug's way keeps exhaust out of your face better than factory.
Thanks Chris! I would be lost without my junk out back---LOL!
No way I could justify buying MF original parts for this beater Bill! I appreciate your comment! Daniel answered the question.
Thank You Gary, still pulling for you two to get home soon!
This is what the muffler looked like when I brought this thing home over 4 years ago now.
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I don't think that was the original one either it was cobbled in and very loose attaching to the engine. Notice the nail stuck through that pipe elbow and what's left of the muffler discharge? That shroud was in bad shape too.
The new one I put on I THINK was some kind of Cub replacement muffler. Seems like it was around 30-35 bucks delivered.
Today I built a crude tunnel cover. Used .040 aluminum since I can get scraps from the racecar guys. I have 1/8" aluminum plate but decided to go with the thinner stuff to make the job easier. Nothing is straight and square on this tractor, so it looks bad. I wanted it one piece though.
Didn't get many pics. Pop riveted together on the tractor. I cut some of that bead material to go around the front and rear sections.
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Removed it from the tractor took off the bead and peeled the plastic off it.
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Scuffed with a scotchbrite and cleaned but the satin black paint job failed. Bad spray bomb. It was drippy and spraying smooth one second then rough the next. Hope to give it a quick sand job and start over with a better can of paint tomorrow afternoon.
No pics of that.
DAC