What are you currently working on??

Worked on the FF24 Saturday, never failed 3 times I went out, hot and sun shining, rain started within 15 mins.
Anyway, im about ready to push this thing in the river, I truly hate Onans. After cleaning the tank, new lines, fuel filter, the pulse pump would pump. Thankfully I had left the electric pump on it so was able to swap lines and get it running, but still wants some choke. I think ive clean that carb 3 or 4 times, once in the Ultrasonic cleaner.

After getting frustrated, I put the tank back in the CC-3184, flushed the line and cleaned fuel filter. It started, but it's hunting also. I pulled carb and took it apart. The emulsion tube has 14 little tiny holes, I bet 10 of them were plugged with the algae garbage that was in the tank. Maybe I'll find time this week to get it installed.
 
A couple weeks ago, I was cutting grass with my 126, and it stopped moving. I finally got to look at it this weekend. I checked the pins in the driveshaft and they were all good. I noticed the shift lever for the creeper gear had no resistance, so I assumed the problem was in there. You have to slide the transmission back to get to it. IMG_1191.jpeg
When I pulled the drain plug out, this fell out, the pin that holds the shift fork to the lever. It wasn’t broken, it just fell out.
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The hole was worn out of round. I drilled it out and put the next size bigger pin in. It seemed to fit tight, hopefully it stays this time.
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I put it back together, and took it for a test drive. I adjusted the brakes too, so it actually stops good now. Everything was good, so I put the mower deck back on and cut grass. It did good until the mule drive belt shredded, and I did not have a spare.
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Finished up with the 1440.
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